This site is not affiliated with AGCO Inc., Duluth GA., Allis-Chalmers Co., Milwaukee, WI., or any surviving or related corporate entity. All trademarks remain the property of their respective owners. All information presented herein should be considered the result of an un-moderated public forum with no responsibility for its accuracy or usability assumed by the users and sponsors of this site or any corporate entity. | ||||||
The Forum | Parts and Services | Unofficial Allis Store | Tractor Shows | Serial Numbers | History |
My 180 laid down |
Post Reply |
Author | |
DMiller
Orange Level Access Joined: 14 Sep 2009 Location: Hermann, Mo Points: 31119 |
Post Options
Thanks(0)
Posted: 01 Sep 2024 at 3:04pm |
Today. Been complaining awhile but the PTO Kicked out hard enough it bent the shift rod alongside the trans. Has slipped out on occasion but this was unexpected. It has been passing Hyd to the Final for awhile so seals, bushing, bearing time likely will need a Shaft and Collet. While split will replace the ailing Clutch, and should a a wild hair grow wilder the engine comes down. Just not a needed due at this point.
Edited by DMiller - 02 Sep 2024 at 4:30am |
|
Sponsored Links | |
Ky.Allis
Orange Level Joined: 31 Jan 2010 Location: Kentucky Points: 1003 |
Post Options
Thanks(0)
|
So, just what are you talking about?
|
|
DougG
Orange Level Joined: 20 Sep 2009 Location: Mo Points: 8110 |
Post Options
Thanks(0)
|
Yeah kinda wondering that too,,,,,
|
|
DMiller
Orange Level Access Joined: 14 Sep 2009 Location: Hermann, Mo Points: 31119 |
Post Options
Thanks(0)
|
Time for the 180 to feel a little love, as did my last two projects. PTO work is least issue, get it down to engine and she will get a refreshing.
|
|
DMiller
Orange Level Access Joined: 14 Sep 2009 Location: Hermann, Mo Points: 31119 |
Post Options
Thanks(0)
|
Sky high balloon texted then we spoke on phone, his own 180 did this where Dr A gave advice, did not see how as little as .001-.003 in burred areas on edges of shaft at shift collar connection would do this but as had the shaft out to inspect did as he had been instructed, filed said burrs back down reassembled and used, amazed.
Credit to Skyhighballoon and Dr Allis. Still has and did confirm shaft internal seal leak y with a friends borescope, but is functional for the few days needed now and then can approach it as a project. |
|
Post Reply | |
Tweet
|
Forum Jump | Forum Permissions You cannot post new topics in this forum You cannot reply to topics in this forum You cannot delete your posts in this forum You cannot edit your posts in this forum You cannot create polls in this forum You cannot vote in polls in this forum |