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Finally got in a good day

Printed From: Unofficial Allis
Category: Allis Chalmers
Forum Name: Construction and other equipment
Forum Description: everything else with orange (or yellow) paint
URL: https://www.allischalmers.com/forum/forum_posts.asp?TID=78780
Printed Date: 28 Jun 2025 at 10:37am
Software Version: Web Wiz Forums 11.10 - http://www.webwizforums.com


Topic: Finally got in a good day
Posted By: DMiller
Subject: Finally got in a good day
Date Posted: 17 Oct 2013 at 7:03pm
Wound up with oil everywhere but what is new. Finally got into the donor enough to get to the trans, by all the 'Red' glue it was out recently.

White paint on Rt rail is master pin, liked to not found the darn things so marked them for later. Dimples were filled with almost concrete like residue. Have been removing anything in the way.
Have to gather up the runner to turn the machine around, the 180 pictured won't do it just digs holes, then I can pull trans and drop rails.



Replies:
Posted By: DMiller
Date Posted: 17 Oct 2013 at 7:06pm
BTW, re-measured rail 28" across four links, almost even. Rear sprocket rings are weld ons but not Allis, not sure whose they are, have been gas axe trimmed at the ears of the sprockets for some reason. So far all but a very few of the rubberized hoses shattered like glass or tore in two.


Posted By: sluggok
Date Posted: 18 Oct 2013 at 2:48am
keep the pictures coming, like to see a project making progress


Posted By: Dozer
Date Posted: 18 Oct 2013 at 5:31am
Very impressive. How many hours do you have into this project? Do you have a helper? Are you going to swap transmissions or are you going to take the doner transmission appart? Keep sending pictures.


Posted By: DMiller
Date Posted: 18 Oct 2013 at 6:40am
As I don't have children and my closer relatives do not live that close I have but three working this project: Me, Myself and I, we stay persistently busy. I have around 48-58 hours so far in the tear down of realistic time, some days do better some days just piddle and stare as I am so tired from my real job. The 180 is my assistant most days but even it complains some, it did not like the weight of the engine/torque converter as a assembly, hydraulics squealed loud when it bound any at all. Even as stripped as it is the old machine is a chunk, 180 would slip tires and dig holes trying to move it,

Plan on doing a trans swap as is, not going to open it up as small parts are slim pickings these days, will open the runner's trans on removal to see what was failing.


Posted By: DMiller
Date Posted: 19 Oct 2013 at 6:52am
Got the runner off the hill and turned the donor around, also got some photos of the lesser shoes that should come off for replacements, have six ID'd so far.



Posted By: DMiller
Date Posted: 19 Oct 2013 at 6:56am
Please excuse the mess in the shed, been kind of busy! Did get four of the worst location bolts out of the trans mounting, these had me worried but came loose with a 3/8" ratchet and universal socket. Have tried to get the lower roller bolts loose but have to get the rails off to get my big impact on them, 1/2" won't budge them.

The bolts were in these locations:



Gonna play hell getting to those locations on the runner.


Posted By: DMiller
Date Posted: 19 Oct 2013 at 7:29pm
Trans is out, have the unit up on supports and lo & behold, the lower rollers are crap, been trimmed on the outer edge, inside edges rolled and eroded to little to nothing, bearings are completely gone to fully locked up and squared the roller faces but the trans is sitting where I need it for now. Went to drive the master pin on right rail, set up a drift guide and bang, three full shots and the head on my sledge fell off, handle broken inside the head, time to regroup.



Posted By: DMiller
Date Posted: 19 Oct 2013 at 7:38pm
One thing I find impressive, with all that is off the machine, the runner's hydraulics won't yet lift the remainder. U-joint is also toast, hope the one in the runner is OK or more parts to find.

Will be pulling both strainers and cleaning EVERYTHING before I go to pull the swapover. One trans pump mount bolt broke off in the aluminum mount, will have to get it out prior to the swap too. May build all the hoses from the pull-outs so I won't have to worry of subsequent failure.


Posted By: DMiller
Date Posted: 21 Oct 2013 at 4:44pm
Ended up with a new handle for the sledge, the one it had would not stop breaking off inside the head, new one did fine. Rails are down, master pins are definitely German, Gutantite they were!! Found the rear sprockets are Henderson, been butch hacked for some reason to taper the teeth. My shoulders are sore from the 20#!



Posted By: Skyhighballoon(MO)
Date Posted: 23 Oct 2013 at 9:30pm
Dave - thanks for sharing!  I sure hope you end up with one real GOOD one put back together when it's all done.   Mike

-------------
1981 Gleaner F2 Corn Plus w 13' flex
1968 Gleaner EIII w 10' & 330
1969 180 gas
1965 D17 S-IV gas
1963 D17 S-III gas
1956 WD45 gas NF PS
1956 All-Crop 66 Big Bin
303 wire baler, 716H, 712H mowers


Posted By: DMiller
Date Posted: 24 Oct 2013 at 4:24am
You and I both!


Posted By: Glockhead SWMI
Date Posted: 25 Oct 2013 at 12:28pm
Good job! Lots of work. Looks fun.



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