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Allis Chalmers electric forklifts |
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Jim.ME ![]() Orange Level ![]() Joined: 19 Nov 2016 Location: Maine Points: 963 |
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If you want to sell it you might have better luck if you post it, as a new post, on the Classifieds Forum; not just on the end of this 9 year old thread.
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bsa101 ![]() Bronze Level ![]() ![]() Joined: 11 Apr 2019 Location: Akron, Ohio Points: 1 |
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I have an ACE50 36 volt that is in wonderful shape, but the battery is about dead ... looking to let it go. It has had VERY little use and looks great!
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Wired ![]() Bronze Level ![]() ![]() Joined: 23 Oct 2018 Location: MI Points: 3 |
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I have done some additional testing, and it is looking like SCR is bad. Anyone on here have a good wiring diagram for 1975 Allis-Chalmers ACE 50 EV? I have a pdf manual, but it has a ton of grammatical errors and really don’t trust most of the specs.
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Ray54 ![]() Orange Level Access ![]() Joined: 22 Nov 2009 Location: Paso Robles, Ca Points: 4756 |
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Welcome Wired
NIKT has not visited since OCT 2011, so hopefully someone else can answer you.
Good that you have some knowledge on forklifts cause that seem a area that knowledge is somewhat limited here. |
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Wired ![]() Bronze Level ![]() ![]() Joined: 23 Oct 2018 Location: MI Points: 3 |
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NIKT, think the POT is working, but going to check today. Problem is the ACE manual I have has lots of grammatical errors, don’t really trust the ohm specs. With meter it says 0-200 ohms min, 5000-4000 ohms Max. Thinking the Max is backwards, and not sure the numbers are right.
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Wired ![]() Bronze Level ![]() ![]() Joined: 23 Oct 2018 Location: MI Points: 3 |
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NIKT, need some help on Allis-Chalmers ACE 50K. Lost reverse & forward at same time. I replaced A1 contactor because it was worn out, and when I manually closed it and activated acclerator I had full speed rverse & forward. However, now looking at the diagram I have I understand A1 is a full speed bypass, which was not working on this ACE. Switch on accelerator pedal is missing metal pivot and does not close switch at WOT, so probably had some speed left that was not using. Anyway. No humming at all when pedaling in reverse or forward, eight fuses I know of are good. Am I into SCR box area?
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VAfarmboy ![]() Silver Level ![]() Joined: 06 Dec 2013 Location: Virginia Points: 470 |
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Your best bet for old manuals is probably ebay.
The seal kit for the tilt cylinder is probably pretty standard if you know the size of the cylinder. You might try Hercules Sealing Products to see if they have a kid that will fit. Edited by VAfarmboy - 26 Sep 2018 at 1:24am |
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CmdrDick ![]() Bronze Level ![]() ![]() Joined: 17 Sep 2018 Location: 34465 Points: 6 |
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Need some help with locating parts for an ACE 30A Electric forklift
Serial number is DCK 502747, that looks like a late 70's vintage. I need a manual, parts book and a link to sources that MIGHT stock parts. Today I need a seal kit for a tilt cylinder, but don't know the part number. This is a great LITTLE machine and exactly what I need for my confined area. Another question. Is the pump supposed to run whenever the key is on, even when non of the controls are activated, mine does.
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Un4givn ![]() Bronze Level ![]() Joined: 23 Apr 2015 Location: Georgia Points: 1 |
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I have a ACE 50A and the drive contactors won't engage. It was left out in the rain and the control compartment filled with water. Does anyone have any advice on how to proceed?
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Loyd ![]() Bronze Level ![]() Joined: 16 Apr 2011 Points: 16 |
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NIKT
Thank you for the reply. I do appreciate it very much. Also thanks for the safety tips. I was a plant manager for 11 years and fully understand the impact that needless accidents cause. Loyd Model # E 50S EV 36 VOLTS |
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NIKT ![]() Bronze Level ![]() Joined: 24 Jun 2010 Location: USA Points: 15 |
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To Anyone: I somehow missed a message asking how to bleed the power steering lines on an A-C electric. Please resend your question and I'll try to help.
NIKT
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NIKT ![]() Bronze Level ![]() Joined: 24 Jun 2010 Location: USA Points: 15 |
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First off- disconnect the battery connector to electrically neutralize the forklift. On an Actronic (transistor control) truck turn on the key switch and press the hornbutton to discharge the control capacitors. Double check with a voltmeter across the (+) and (-) power leads to be sure there is no voltage present. On an EV-1 (SCR control) truck you must open the control compartment door and very carefully short the two threaded terminals on top of the capacitor of the control unit. You may get a strong, loud spark.
Now, open up and remove the floorboard and toe plate. You will likely have to remove the contactor panel cover and any shrouds that are below and just ahead of the driver's seat assembly. Depending on the model forklift and its size, you should now be able to see the commutator-end (the back end) of the drive motor and the screened (sometimes solid) coverbands. This is where the brushes are.
Again, depending on truck model, you should be able to reach under and remove/replace the brushes on the bottom. The brushes are typically on a 45-degree angle and are accessible. If you must raise the forklift to reach the lower brushes, do so with EXTREME care. If not properly blocked a forklift can slip loose and crush and KILL you. I have done investigations on forklift accidents, including A-Cs, and the sight is horrendous and the loss to loved ones is devastating. Good luck!
NIKT
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Loyd ![]() Bronze Level ![]() Joined: 16 Apr 2011 Points: 16 |
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if anyone is still around.....what is the easiest way to change brushes on the main drive motor on a allis electric forklift?
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Loyd ![]() Bronze Level ![]() Joined: 16 Apr 2011 Points: 16 |
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if anyone is still around.....what is the easiest way to change brushes on the main drive motor on a allis electric forklift?
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RadarMan ![]() Bronze Level ![]() Joined: 08 Oct 2010 Location: Alaska Points: 1 |
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USAF/Allic Chalmers Model # ACE 45 EV EE has issues. When shifted into forward or reverse, truck will not initially engage drive wheels when the pedal is depressed. After a short period of time, the wheels engage and work fine until shifted into neutral or a change of direction is applied. Then, the same thing occurs in the other direction. Of special interest is that, when in forward or reverse with the pedal depressed, activation of the lift or tilt cylinder will help to engage the drive.I have lifted the drive wheels and tested. The drive works fine without load in both directions back and forth. There does not seem to be any hesitation with the drive wheels off the ground.
My first thoughts were the direction sensor or the drive potentiometer. After the wheels up test, I am not so sure about this.
Any comment?
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Jimmy Forklift ![]() Bronze Level ![]() Joined: 05 Sep 2010 Location: Alberta Points: 6 |
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NIKT:
She works damn good. Gotta replace the cylinder seals at some point, but not too concerned about the minor leaks. ☺
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oldfoolstools ![]() Bronze Level ![]() Joined: 26 Jul 2010 Points: 7 |
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NIKT
Sorry about the late reply.
I have benn experiencing some computer problems. Yes, I would like a copy of the SCR manual. Email me at randall@aerospacetooling.com. Thank you so much for your help.
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NIKT ![]() Bronze Level ![]() Joined: 24 Jun 2010 Location: USA Points: 15 |
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To Jimmy Forklift,
How is your unit working so far?
To Oldfoolstools,
I finally found a copy of a complete General Electric technical manual. Do you still need SCR control info? If so, give me an email address so I can send it to you.
NIKT
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NIKT ![]() Bronze Level ![]() Joined: 24 Jun 2010 Location: USA Points: 15 |
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To Jimmy Forklift,
I really like your ingenuity in fabbing up and installing a brush-box support ring. Just so you know, Warfield Electric does stock rebuild parts, including armatures, fields brush rigging and brushes, terminals, and other parts for motors in A-C and just about any forklift you can name.
The fact that your power steer motor seems to run fast (screaming at light loads) and seems to overheat may indicate that the field windings have turn-to-turn shorts and this will make the motor run at high speed. The current draw at light loads (steering wheel with no steering input) should be about 10-15 Amps. With steer wheels against the stops and at hydraulic relief pressure, current should be 35-50 Amps. When convenient, you may want to pull the motor and have a local (good) starter-generator repair shop check the armature and fields. If your budget and time permit, you might check with Warfield Electric or even send it to them for test and repair. I tout these guys because I have seen them work miracles on motors that looked like hopeless cases. Like you, though, my first choice would be to try to fix it myself.
Keep up the good fight.
NIKT
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Jimmy Forklift ![]() Bronze Level ![]() Joined: 05 Sep 2010 Location: Alberta Points: 6 |
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Forgot to mention...
Barnes and Co. was bought out by Haldex.
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Jimmy Forklift ![]() Bronze Level ![]() Joined: 05 Sep 2010 Location: Alberta Points: 6 |
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NIKT:
Yes, I lubed the coupling you refer to. My pump was made by Barnes and Co., as it is still stamped as such. The motor looks like it has been serviced or replaced... not sure. But there is a stamp on it from previous service work by a local company (I bought it used).
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Jimmy Forklift ![]() Bronze Level ![]() Joined: 05 Sep 2010 Location: Alberta Points: 6 |
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NIKT;
Yes, the commutators were grooved, and when I initially removed the entire motor for service, I spun the comm's on our lathe at work and then scored the mica. The comm's are not perfect..... but it now works quite well.
One thing I noticed when the motor first went was that I was able to have power steering for about an hour or so and the machine was perfectly quiet, then it got harder to steer and gradually the PS deteriorated. Since the PS motor in this unit is so loud, I decided to put a switch in line from the ignition to the PS coil (clapper), so I can run the machine quietly for a short time if need be. Really, for my use all I need is short bursts to load and unload delivery trucks.... not using this thing in a warehouse.
I also did one other repair.... when we had the forklift elevated, I noticed that the main drive motor brushes were sitting at an angle. What happened was the bake-lite piece that holds the brush guides had broken, and the outer ring and brushes were acutally floating around.
I made a new ring out of fiberglass, machined it to the right thickness, bored the center hole, bought new brushes, and man this thing operates nice now. The bake-lite is actually not that strong, so I was surprised AC used it back in the day. Perhaps no other material was available. The fiber ring with about 12 layers of 2 oz matting (5/16" thick) and resin is so strong that it will outlive me.
Anyway, another solution available to anyone that comes across the same problem.
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NIKT ![]() Bronze Level ![]() Joined: 24 Jun 2010 Location: USA Points: 15 |
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To Jimmy Forklift,
Some more thoughts on your project: That little couple you described is called an "Oldham Coupling" and acts like a mini U-joint to take care of any misalignment. It should be lightly lubed before assembly.
Most of the pumps of that era were made by the Barnes company in Rockford, IL, and the motors were supplied by Prestolite. Both the companies have been bought and sold a couple of times, so I'm not sure of their present corporate names. You can easily obtain motor parts(for sure) and pump parts (possibly), from Warfield Electric at 815-469-4094.
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NIKT ![]() Bronze Level ![]() Joined: 24 Jun 2010 Location: USA Points: 15 |
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To Jimmy Forklift, Good detective work. On a 2-terminal motor with wound (coils of wire) fields, if you reverse polarity of the supply voltage, the motor will always rotate in the same designed direction. To reverse such a motor, you must reverse the field connections or the armature connections, but not both.Evidently, when you changed the brushes the first time, you did, as you correctly analyzed, inadvertantantly changed the armature connections causing reverse rotation.
It is the usual practice to drop the pump motor out for service. You then should be able to remove the brush cover band and replace the brushes without having to disconnect all the brush cross-connectors.
By the way, since the brushes were so badly worn, was the commutator OK? If it was scored or grooved, then you may want to disassemble the motor and have the commutator trued and resurfaced and the mica undercut.
I'm glad if I was any help on your project.
NIKT
PS to oldfoolstools,
Did you get your rig going? Sad to say no one came through with an A-C schematic, so I'm trying to find a generic GE SCR schematic. Let us know how you have done. |
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Jimmy Forklift ![]() Bronze Level ![]() Joined: 05 Sep 2010 Location: Alberta Points: 6 |
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Hi all. I figured out my errors and am posting this update just so that the info may be useful to someone else someday. As mentioned, my power steering motor quit when the brushes in the DC motor wore down to nothing. I removed the motor from up underneath the rear axle and replaced the brushes. This motor had 4 brushes, with two contact points to the outer DC connecting bolts. The brush harness is in a T configuration, with one set of brushes connecting to one lug and feeding opposite sides of the commutators (180 degrees), and the second T brush feeding similar. Therefore, all 4 brushes are on the comm's spaced every 90 degrees. The length of the harness off of the center of each T is not the same, which is what causes variable current to hit the comm's and affect rotation direction. NOTE that the two 48 volt wires (+,-) feeding the body of the motor do nothing to affect rotation when exchanged.When I reinstalled the brushes, I didn't take note of the direction of the longer leads in the T and where they were, so I obviously installed them backwards and my motor spun backwards. After correcting, the motor now spins the proper direction and power steering works excellent.
To note: The proper direction for the pump on this machine is clockwise rotation when looking at the shaft of the pump (where it connects to the motor). The fluid inlet is on the bottom, pressure outlet is on the top of the pump.
The reason I was not getting power steering to work after I initially installed the new brushes, then changed them and tested, was because when I went and changed them, I did so by not removing the entire motor from underneath the rear axle. I just pulled off the back end of the motor housing where the brushes are, and switched them there.
PROBLEM WAS.... when I did so, I must have pulled on the armature slightly and it pulled away from the pump a little, dislodging the armature key. So when I retested the motor with the brushes changed, the motor wasn't turning the pump and it was at that point that I thought I was going nuts. I finally had enough and took it all out again, only to find the key sitting in the bottom of the motor housing and me feeling rather stupid.
In short, if your power steering needs servicing, elevate the rear of this model forklift (ON BLOCKS, safety first) and remove the entire unit because if my experience with the armature KEY is standard factory, then this is not like anything I've ever seen. Most keys are insterted in the side of a shaft, but not this one. It is a little round extension, male on one side, female slot on the other side, keyed into the end of the armature shaft and mates with the pump. My pump still has an Allis Chalmers stamp on it, so I believe my entire setup is still factory.
At any rate, reading NIKT above shed some help about these forklifts for me, which was useful. Hopefully my crazy experience will help someone else by reading this.
All the best.
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Jimmy Forklift ![]() Bronze Level ![]() Joined: 05 Sep 2010 Location: Alberta Points: 6 |
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Hello: I've got an older AC ACE 40A 48 Volt electric forklift. Everything was working excellent until the power steering motor quit. The brushes wore out so I removed the motor and replaced (4 brush model). I reinstalled and am having a tough time getting steering to work. Is there a special process for priming or bleeding the lines? Someone told me that I may have put the brushes back in incorrectly and the armature is turing the wrong direction. Anyone know which way the armature should turn? I've tried both directions and am having a hard time getting steering back to where it was.Any suggestions would be appreciated.
BTW... the resevoir is full, the feed lines are not crushed, the battery is excellent, all other hydraulic functions work fine.
Thanks.
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NIKT ![]() Bronze Level ![]() Joined: 24 Jun 2010 Location: USA Points: 15 |
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OK. Keep me posted. NIKT |
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oldfoolstools ![]() Bronze Level ![]() Joined: 26 Jul 2010 Points: 7 |
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NIKT
Thanks again
The drive motor does not work at all in reverse or fwd with the both contactors engaged.
Reverse worked for a short time using the pedal, but was noisy and not at a constant speed. I will check the continuity on the motor terminals as soon as I get a chance. I have gotten busy here at work with some other issues. I will also try the test on the steering. I may possibly have a broken piston i the hyd cylinder as this machine had been forcibly moved around sevral times with another forklift. R
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NIKT ![]() Bronze Level ![]() Joined: 24 Jun 2010 Location: USA Points: 15 |
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Hi oldfoolstools, I am disappointed that I haven't yet found a schematic, but I haven't given up.I see we have at least two problems to solve--one, the drive system, and, two, the power steer system.
Let's keep chugging along here while my A-C pals keep digging for a wiring diagram.
Drive System: Would you please clarify one more time--If you manually close both the Forward contactor and the 1-A bypas contactor, does the drive motor run? And does the motor run with the Reverse contactor and the 1-A both closed? If the motor doesn't run under these conditions, then there is an open in the drive power circuit.
You can check motor continuity: With all cables disconnected from the motor, there should be continuity from S1 to S2 (letters stamped into field ring). These are the series field coils. Note: some field terminals were marked F1 and F2, so keep an eye open for this. The armature terminals should be marked A1 and A2. Both the armature and field windings in the motor should have a low resistance, typical HUNDRETHS of an ohm. Usually the the fields almost never fail, but a shorted field coil(s) wold tend to make a running motor want to run faster, but pull an abnormally high current and while causing much brush sparking. If there is no armature continuity, you may have stuck or worn brushes. Remove the cover bands at the brush-end of the motor and take a look. If the brushes seem to be well down into, or flush with the brushboxes, they are definitely worn out. Brushes and all motor parts are readily available from people like Warfield Electric Co, 815-469-4094 for reasonable prices.
Power steer problem: This sounds like a hydraulic problem. If the lift and tilt work OK, then the odds are the fluid level is OK. Since the power steer motor seems to run OK, then you may have a hose or component problem. Check the hose that feeds the inlet port of the power steer pump to make sure it is not collapsing from suction vacuum. It may help to know how this system works: This system is a full power assisted sytem with no mechanical link between the steering wheel and the small diameter steerable wheels located at rear of the forklift. The power steer pump sends fluid to an Orbitrol valve controlled by the steering wheel. There are four ports in the steer valve--the inlet port gets pressurized fluid from the pump, while two of the ports are connected to the power steer cylinder. When you turn the steering wheel to the left or right, fluid is directed to one side or the other of the power steer cylinder to move its piston one way or the other to steer left or right. The fourth port on the Orbitrol is the drain line back to the reservoir. I would suggest pulling the drain line that goes from the Orbitrol drain port to the tank, and aim it into a deep bucket. Run the power steer motor briefly to see if fluid is being pumped at all. Assuming there is sufficient fluid in the tank, if there is no flow, then the suction hose may be collapsed or a filter may be clogged. Usually a suction side restriction will result in pump cavitation and cause a high pitched noise. If you have good flow in the drain line, turn the steering wheel to see if the steer cylinder and linkage move. If not, try to raise the steer wheels off the ground and repeat the test. If the wheels then steer, you may have an abnormally steering low relief pressure. The relief valve is typically built into the power steer pump. You should set relief pressure with a gauge as you could blow the lines with excess pressure. You should hear the power steer motor/pump unit speed up and slow down as you steer , and you should hear the unit run slower when you get to either end of the stroke of the power steer cylinder. If you get thes audible clues, but the no steering, you may have a rare case of the piston breaking loose from the piston rod and just moving back and forth in the cylinder without doing any steering.
Try these hints and let me know how you make out.
NIKT
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oldfoolstools ![]() Bronze Level ![]() Joined: 26 Jul 2010 Points: 7 |
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Hi NIKT Thanks for your reply. I had already checked all the items you mention before I contacted you the first time. You are very thorough!
The Battery is fully charged 36 + volts and checked again under a load. No dead cells. Lift Motor runs and lift tilt and side shift all work. The Steering Pump motor runs, but the wheels do not turn left or right. I am assuming this to be a hydraulic unit using the same reservoir as the lift pump. Maybe I have a bad hyd cylinder or steering valve.
Fuses are all good
The seat switch is good
The directional switch is good
The accelerator switch is good
Contactors for reverse, forward, and the smaller contactor that closes upon turning on the machine all actuate and have continuity.
I pulled all the drive motor wires off one at a time and cleaned the connections.
I had already blocked up the wheels to test and tried manually actuating the contacts although they worked fine with the accelerator.
At one point I got reverse to work for a short time, but not forward. When it ran in reverse the motor seemed to speed up and down and made a growling noise. At this point I am thinkig as you said that it is a worn motor brush problem. Are these still available? Is there a continuity check that could affirm this?
Hope this helps. Thank you so much for your time. R.
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